In order to reduce the pressure head well surface level of the explosion well 5 in Baghjan, the process for restoring the deviation of gas flow from the head of the well Baghjan EPS and two wells flares was applied with today.Today successful operation was then brought expert Alert M / s OIL completed testing / inspection of the wellhead and safety inspection with the safety analysis of specific use of system-wide today. The gas flow was diverted to EPS around 8.40 hours after closing the BOP and burning a portion of the gas that was diverted to two wells of flares.
Thepressures of the well head and related parameters are constantly monitored and once the entire system is stabilized, the next line of action will be carried out by killing the exploitation of wells. All security measures are in place and the head of the well, BOP stack, pincher manifold and ground X-Mas tree are being continuously sprayed water for cooling purposes. They are taking all efforts to control the well as soon as possible.